Thanks David!
I finally made it out today for another maiden flight. I consider the first few flight's the maiden as well because of the changes being made to the airframe such as adding weight of which changes the flight characteristics. So, I arrived this morning in high spirits of another flight. Only to have them squashed like a bug. Flip after flip of the prop yielded the engine to being so flooded gas was dripping out of the cowl. After checking as much as I could there at the field I finally conceded to packing it up. After arriving home I unloaded the plane from the trailer, removed the prop and cowl. Everything was plugged in so I removed the plugs, they were still wet with fuel. I dried the plugs, snapped them into the caps, turned everything on, and flipped. Arggghhh, no fire! What the hadez, I thought to myself and comensed to checking the electronics via a tester. I had power all the way up to the ign module. Now, being as there has been nothing that would have caused the module to just go out I was getting pretty angry by this point. Deciding to sit and have a smoke whilst cooling the head sounded good, about the time I reached for the smokes a light went off. OMG, really, could it be that? Shiet! Remember when I had to remove the tele module to re-download the program on my LT? Well, when I re-installed it into the airframe I reversed the harness for the rpm. The harness is modified at the module end but normal at the other and by reversing it I essentially cut power to the module.
That's my story and I'm sticking to it.
That's all folk's! Will try again tomorrow.